From: Aaro Koskinen Date: Tue, 5 Mar 2013 11:04:23 +0000 (+0200) Subject: usb: musb: omap2430: fix omap_musb_mailbox glue check again X-Git-Tag: v3.9-rc3~17^2~7^2~3 X-Git-Url: http://review.tizen.org/git/?a=commitdiff_plain;h=f8c4b0e73b636fe06e8283f29905c2e60ed66fa1;p=profile%2Fivi%2Fkernel-x86-ivi.git usb: musb: omap2430: fix omap_musb_mailbox glue check again Commit 80ab72e1 (usb: musb: omap2430: fix the readiness check in omap_musb_mailbox) made the check incorrect, as we will lose the glue/link status during the normal built-in probe order (twl4030_usb is probed after musb omap2430, but before musb core is ready). As a result, if you boot with USB cable on and load g_ether, the connection does not work as the code thinks the cable is off and the phy gets powered down immediately. This is a major regression in 3.9-rc1. So the proper check should be: exit if _glue is NULL, but if it's initialized we memorize the status, and then check if the musb core is ready. Signed-off-by: Aaro Koskinen Signed-off-by: Felipe Balbi --- diff --git a/drivers/usb/musb/omap2430.c b/drivers/usb/musb/omap2430.c index 1762354..2a39c11 100644 --- a/drivers/usb/musb/omap2430.c +++ b/drivers/usb/musb/omap2430.c @@ -237,9 +237,13 @@ void omap_musb_mailbox(enum omap_musb_vbus_id_status status) { struct omap2430_glue *glue = _glue; - if (glue && glue_to_musb(glue)) { - glue->status = status; - } else { + if (!glue) { + pr_err("%s: musb core is not yet initialized\n", __func__); + return; + } + glue->status = status; + + if (!glue_to_musb(glue)) { pr_err("%s: musb core is not yet ready\n", __func__); return; }