From: Adam Ford Date: Sat, 12 Jan 2019 23:32:00 +0000 (-0600) Subject: ARM: imx6q_logic: Correct phy fixup for broken ethernet X-Git-Tag: v2019.04-rc2~9^2~46 X-Git-Url: http://review.tizen.org/git/?a=commitdiff_plain;h=8dd0dff2695cd6f6f863af37a53a042724f5b263;p=platform%2Fkernel%2Fu-boot.git ARM: imx6q_logic: Correct phy fixup for broken ethernet The Ethernet has been broken for some time. This patch unifies this board with a few others that use a similar approach to enabling phy. This fixes ar8031 Ethernet controller so it works. Signed-off-by: Adam Ford --- diff --git a/board/logicpd/imx6/imx6logic.c b/board/logicpd/imx6/imx6logic.c index 89cf53c..b17a3b1 100644 --- a/board/logicpd/imx6/imx6logic.c +++ b/board/logicpd/imx6/imx6logic.c @@ -60,57 +60,6 @@ static iomux_v3_cfg_t const uart3_pads[] = { MX6_PAD_EIM_EB3__UART3_RTS_B | MUX_PAD_CTRL(UART_PAD_CTRL), }; -#ifndef CONFIG_SPL_BUILD -static void fixup_enet_clock(void) -{ - struct iomuxc *iomuxc_regs = (struct iomuxc *)IOMUXC_BASE_ADDR; - struct gpio_desc nint; - struct gpio_desc reset; - int ret; - - /* Set Ref Clock to 50 MHz */ - enable_fec_anatop_clock(0, ENET_50MHZ); - - /* Set GPIO_16 as ENET_REF_CLK_OUT */ - setbits_le32(&iomuxc_regs->gpr[1], IOMUXC_GPR1_ENET_CLK_SEL_MASK); - - /* Request GPIO Pins to reset Ethernet with new clock */ - ret = dm_gpio_lookup_name("GPIO4_7", &nint); - if (ret) { - printf("Unable to lookup GPIO4_7\n"); - return; - } - - ret = dm_gpio_request(&nint, "eth0_nInt"); - if (ret) { - printf("Unable to request eth0_nInt\n"); - return; - } - - /* Ensure nINT is input or PHY won't startup */ - dm_gpio_set_dir_flags(&nint, GPIOD_IS_IN); - - ret = dm_gpio_lookup_name("GPIO4_9", &reset); - if (ret) { - printf("Unable to lookup GPIO4_9\n"); - return; - } - - ret = dm_gpio_request(&reset, "eth0_reset"); - if (ret) { - printf("Unable to request eth0_reset\n"); - return; - } - - /* Reset LAN8710A PHY */ - dm_gpio_set_dir_flags(&reset, GPIOD_IS_OUT); - dm_gpio_set_value(&reset, 0); - udelay(150); - dm_gpio_set_value(&reset, 1); - mdelay(50); -} -#endif - static void setup_iomux_uart(void) { imx_iomux_v3_setup_multiple_pads(uart1_pads, ARRAY_SIZE(uart1_pads)); @@ -141,8 +90,33 @@ static void setup_nand_pins(void) imx_iomux_v3_setup_multiple_pads(nand_pads, ARRAY_SIZE(nand_pads)); } +static int ar8031_phy_fixup(struct phy_device *phydev) +{ + unsigned short val; + + /* To enable AR8031 output a 125MHz clk from CLK_25M */ + phy_write(phydev, MDIO_DEVAD_NONE, 0xd, 0x7); + phy_write(phydev, MDIO_DEVAD_NONE, 0xe, 0x8016); + phy_write(phydev, MDIO_DEVAD_NONE, 0xd, 0x4007); + + val = phy_read(phydev, MDIO_DEVAD_NONE, 0xe); + val &= 0xffe3; + val |= 0x18; + phy_write(phydev, MDIO_DEVAD_NONE, 0xe, val); + + /* introduce tx clock delay */ + phy_write(phydev, MDIO_DEVAD_NONE, 0x1d, 0x5); + val = phy_read(phydev, MDIO_DEVAD_NONE, 0x1e); + val |= 0x0100; + phy_write(phydev, MDIO_DEVAD_NONE, 0x1e, val); + + return 0; +} + int board_phy_config(struct phy_device *phydev) { + ar8031_phy_fixup(phydev); + if (phydev->drv->config) phydev->drv->config(phydev); @@ -160,9 +134,6 @@ int overwrite_console(void) int board_early_init_f(void) { -#ifndef CONFIG_SPL_BUILD - fixup_enet_clock(); -#endif setup_iomux_uart(); setup_nand_pins(); return 0;